天津科技 ›› 2025, Vol. 52 ›› Issue (12): 98-100+105.

• 应用技术 • 上一篇    下一篇

“海洋石油112”浮式生产储卸油装置跨接软管国产化替代的应用研究

孟祥伟, 赵金亮, 王汇   

  1. 中海石油(中国)有限公司天津分公司 天津 300459
  • 收稿日期:2025-11-03 出版日期:2025-12-25 发布日期:2026-01-05

Application research on localized replacement of jumper hoses for FPSO “HYSY 112”

MENG Xiangwei, ZHAO Jinliang, WANG Hui   

  1. Tianjin Branch,CNOOC <China>Co.,Ltd.,Tianjin 300459, China
  • Received:2025-11-03 Online:2025-12-25 Published:2026-01-05

摘要: 渤海曹妃甸油田核心浮式生产储卸油装置(FPSO)“海洋石油112”通过3条跨接软管与单点系泊系统(SPM)连接,承担着原油、注水等介质输送“动脉”的职责。原跨接软管由法国Technip公司生产,自2014年投入使用以来,已达到10年设计寿命,存在生产液侵蚀、动态疲劳等安全隐患。受国际形势影响,原厂供货周期长达1年以上且成本高昂,严重制约油田产能释放与安全生产。在此背景下,曹妃甸作业公司通过技术攻关与流程创新,使项目实现三大突破:国内首次生产应用API 17K结构型式大尺寸、大跨度35.6 cm×55 m跨接软管;创新“限液不停产”工艺,将施工周期从6 d压缩至60 h;构建“多设施协同”管理模式,实现零事故高效作业。项目节约采购成本1 500万元,供货周期缩短4个月,形成了覆盖技术研发、生产组织、现场管理的完全解决方案,为海洋石油装备国产化提供了可复制的技术路径与实施样本。

关键词: 跨接软管, 国产化替代, 限液不停产更换, 技术攻关

Abstract: The “HYSY 112”,the core Floating Production Storage and Offloading unit (FPSO) of the Caofeidian Oilfield in the Bohai Sea,is connected to the single-point mooring system via three jumper hoses,serving as the “artery” for the transportation of media such as crude oil and water injection. The original jumper hoses,manufactured by Technip France,have been in service since 2014 and have reached their 10-year design life,with potential safety hazards such as produced fluid corrosion and dynamic fatigue. Affected by the international situation,the original equipment manufacturer (OEM) has a lead time of over one year with high costs,which seriously restricts the production capacity and safe operation of the oilfield. Against this backdrop,Caofeidian Operating Company has achieved three major breakthroughs in the project through technological research and process innovation: realizing the first domestic production application of large-size,long-span jumper hoses with a specification of 35.6 cm×55 m conforming to the API 17K design standard;innovating the “liquid-restricted but non-shutdown” construction technology,cutting the construction period from 6 days to 60 hours;establishing a “multi-facility coordination” management model,achieving zero-accident and high-efficiency operations. The project yielded cost savings of 15 million CNY in procurement and shortened the supply cycle by 4 months,and developed a comprehensive solution covering technology research and development,production organization,and on-site management,providing a replicable technical path and implementation model for the localization of offshore oil equipment.

Key words: jumper hose, localized replacement, liquid-restricted but non-shutdown replacement, technical breakthrough

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